Resources

Consult our range of free resources.

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Technical Guides

Tetra has published a series of guides which are available for ordering.

HRSG Inspection Planning Guide (2nd Edition)

Inspection is part of routine maintenance for any Heat Recovery Steam Generator (HRSG). Visual inspections are performed at regular intervals in accordance with the requirements of regulatory bodies and insurers.Inspection is part of routine maintenance for any Heat Recovery Steam Generator (HRSG). Visual inspections are performed at regular intervals in accordance with the requirements of regulatory bodies and insurers.

HRSG Tube Failure Diagnostic Guide (3rd Edition)

Heat Recovery Steam Generator (HRSG) tubes provide the media for extraction of useful energy from the waste heat in gas turbine exhaust at combined cycle power plants (GT-CCs) or from heat generated by process streams at petrochemical facilities.

Technical White Papers

A selection of technical papers available for reference.

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Visual HRSG Inspections

Visual HRSG Inspections

The predominant technique for inspecting HRSGs is visual. Visual inspection is performed at nearly every...

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Tube Metallurgical Analysis

Tube Metallurgical Analysis

What is normally included in a metallurgical analysis? Visual examination may be obvious, but there is a ...

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Pipevue 2.0

Pipevue 2.0

PipeVue 2.0  PipeVue 2.0 has been specifically developed by Tetra Engineering to store and organize the large ...

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Surface Replica Testing

Surface Replica Testing

Preparation of surface replicas is considered a type of visual test. It has proven to be a valuable tool...

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Sulphuric Acid Dewpoint Corrosion

Sulphuric Acid Dewpoint Corrosion

The key factor in determining rate of cold-end deposits in HRSGs firing natural gas is the sulphuric acid dew ...

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HRSG Inspection Frequency

HRSG Inspection Frequency

Effective maintenance scheduling and planning is critical to completing required work during outages and preve...

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To discuss how we might assist you to improve your plant's performance or to maintain its value over time

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Papers, Presentations and Articles

Selected papers, presentations and articles from major industry conferences and events.

Title
Author
Cost of Cycling Operation-Assessing Radiant Oil & Gas Fired Power Plants
Cost of Cycling Operation-Assessing Radiant Oil & Gas Fired Power PlantsCost of Cycling Operation-Assessing Radiant Oil & Gas Fired Power Plants
D. Moelling, A. Cozza, (Tetra ) and C. Pillar (Scientech)
Dec 2002, POWERGEN INT. in Orlando Flordida USA
Cycling Experience of Large HRSGs in the New England ISO
Cycling Experience of Large HRSGs in the New England ISOCycling Experience of Large HRSGs in the New England ISO
D. Moelling, F. Berté, P. Jackson et.al. (Tetra)
2001, POWERGEN EUROPE Brussels
Case Studies in Maintaining Piping Reliability by Economical Predictive Methods for Inspection Planning
Case Studies in Maintaining Piping Reliability by Economical Predictive Methods for Inspection PlanningCase Studies in Maintaining Piping Reliability by Economical Predictive Methods for Inspection Planning
P. Jackson, D. Moelling, F. Anderson (Tetra)
2001 EPRI International Maintenance Conference, Houston
Application of Quantitative Analysis Techniques to HRSG Erosion-Corrosion
Application of Quantitative Analysis Techniques to HRSG Erosion-CorrosionApplication of Quantitative Analysis Techniques to HRSG Erosion-Corrosion
D. Moelling, F. Anderson, M. Taylor (Tetra)
1999, EPRI Maintenance Conference, Atlanta, GA.

Previous Projects

With over 30 years of experience in power and industrial steam generation services, Tetra Engineering has along history of projects.

Flow Accelerated Corrosion Risk Assessment, 2017
South East Asia

Flow Accelerated Corrosion Risk Assessment, 2017

An assessment of the susceptibility of HRSG piping components was performed according to Tetra Engineering’s FACRisk™ methodology which includes the use of thermal modelling simulation software (PPSD). From each system, sub groups are ranked using both time to minimum wall thickness and wear rate. The highest risk components (such as elbows, tees and valves) are identified. Overall, due to relatively high operating pH level (>9.2), the overall risk of FAC failures at the CCGT plant in question was considered to be relatively low, with few specific areas showing increased risk. Three separate load cases were simulated and analysed to determine the potential FAC risk. The results of each simulation were incorporated into the final locations recommended for inspection.

Boiler Tube Failure Root Cause Analysis, 2017
Asia

Boiler Tube Failure Root Cause Analysis, 2017

After several tube failures in recent years in the 1st row of LTRH hanger tubes, Tetra was tasked with performing a Root Cause Analysis (RCA) to determine the underlying cause of the failures. A detailed review of operating data, failure reports and design information was carried out and potential causes investigated. The tube failure mechanism as determined by metallurgy was short-term overheating, with temperatures likely exceeding 700°C prior to failures. Two contributing causes were identified by elimination of all other possibilities: temporary loss of steam flow in affected leading row tubes coupled with high flue gas temperatures in certain tubes at the side of the boiler gas path.  Unfortunately, the underlying root cause of the loss of flow could not be confirmed, whereas the asymmetric flue gas temperature distribution is a known issue since commissioning.

HP Evaporator Tube Failure Analysis, 2016
Middle East

HP Evaporator Tube Failure Analysis, 2016

During a recent condenser tube leak at a CCGT Power Station in the Middle East, two trips occurred on the boiler feedwater pumps leading to trips of one of the HRSGs.  During that time, three tubes failed on the HP Evaporator. Tetra Engineering performed an investigation into the failures with the aim of determining the failure mechanism, to estimate the root cause of failure, and to identify inspection priorities in case damage may have gone undetected. This work included metallurgical analysis and a review of key operating data. Failures were located directly under the risers at extreme ends of the HP Drum. The most probable source of tensile overload is tube quenching when flow restarted

Attemperator Sleeve Failure Study, 2016
Europe

Attemperator Sleeve Failure Study, 2016

In 2015, it was discovered that the thermal sleeve in the attemperator in a client’s power station hot reheat line had failed, resulting in fracture around the circumferential weld in the sleeve’s mid section. For this reason, Tetra was engaged by the owner to investigate. The investigation showed failure from fatigue cracking. There were no signs of thermal fatigue damage, hence quenching from over-spraying was discounted as the root cause. The cracked area showed signs of high cyclic local strain, and given the moderate number of starts low-cycle fatigue was thought to be the root cause. Differential thermal expansion between the Grade 22 sleeve and the Grade 91 pipe, combined with lock-in of the sleeve on the pin locations, would raise sufficiently high stresses

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