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Guides techniques

Tetra a publié une série de guides qui peuvent être commandés.

HRSG Inspection Planning Guide (2nd Edition)

Inspection is part of routine maintenance for any Heat Recovery Steam Generator (HRSG). Visual inspections are performed at regular intervals in accordance with the requirements of regulatory bodies and insurers.

HRSG Tube Failure Diagnostic Guide (3rd Edition)

Heat Recovery Steam Generator (HRSG) tubes provide the media for extraction of useful energy from the waste heat in gas turbine exhaust at combined cycle power plants (GT-CCs) or from heat generated by process streams at petrochemical facilities.

Article Techniques

Une sélection de documents techniques disponibles à titre de référence.

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Creep Classification of Grade 91 Steel

Creep Classification of Grade 91 Steel

Background Grade 91 steel is superior to many other industry used materials for its increased resistance to m...

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Power Boiler Piping

Power Boiler Piping

Boiler piping design requirements is divided into internal and external jurisdictions. These are divided...

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Welding Procedure Specification (WPS)

Welding Procedure Specification (WPS)

Before any welding activity can commence, the welder and the QC Engineer has to be fully aware of the content ...

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Water Chemistry in HRSGs

Water Chemistry in HRSGs

The environment on the inside of HRSG tubing is an important factor in maintaining tube integrity. The c...

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HRSG Inspection Planning

HRSG Inspection Planning

Building a good inspection plan for the HRSG involves doing the following: Set the Time and General Schedul...

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Tube Failures related to Water Chemistry

Tube Failures related to Water Chemistry

Most corrosion induced tube failures have a component that is directly related to water chemistry. The c...

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Articles, présentations et articles

Sélection d'articles, de présentations et d'articles issus de conférences et d'événements majeurs de l'industrie.

Title
Author
HRSG Purge Credit Case Studies Justifying ROI
HRSG Purge Credit Case Studies Justifying ROIHRSG Purge Credit Case Studies Justifying ROI
Jackson P.
Presented at the 501 User Conference, February, 2019
Lessons Learned from Implementing of ASME B31.1 Chapter VII Operation & Maintenance
Lessons Learned from Implementing of ASME B31.1 Chapter VII Operation & MaintenanceLessons Learned from Implementing of ASME B31.1 Chapter VII Operation & Maintenance
Jackson P.
Presented at the NAES O&M Manager Conference, Houston, TX, February, 2019
Observations on HRSG Tube Module Weld Quality
Observations on HRSG Tube Module Weld QualityObservations on HRSG Tube Module Weld Quality
Taylor M.
HRSG User Group, Nottingham, UK, November 2017
Using Thermohydraulic Simulations to Assess HRSG Performance
Using Thermohydraulic Simulations to Assess HRSG PerformanceUsing Thermohydraulic Simulations to Assess HRSG Performance
Monnac J-M.
Power Magazine, February 2019
Root Cause Failure Analysis of Superheater Tubes Using Computational Fluid Dynamics.
Root Cause Failure Analysis of Superheater Tubes Using Computational Fluid Dynamics.Root Cause Failure Analysis of Superheater Tubes Using Computational Fluid Dynamics.
Fabricius A., Moelling D., Rusaas J.
PowerGen Asia Conference Proceedings, Seoul, South Korea, September, 2016.

Projets Récents

Avec plus de 30 ans d'expérience dans les services de production d'électricité et de vapeur industrielle, Tetra Engineering a une longue histoire de projets.

CFD Analysis of failed 180° Bend, 2013
Middle East

CFD Analysis of failed 180° Bend, 2013

A CFD study on one of the 4th quadrant pipe bends at a thermal power plant steam boiler was performed. The purpose of the analysis was to analyse the change in flow velocity due to an increase in the bend nominal size from 3” to 4”. The connecting pipe run was kept at 3” and standard expander/reducers are used to join the pipe with the bend. Input process parameters were taken from a PPSD model.

LP Economiser Header Failure Analysis, 2010
Middle East

LP Economiser Header Failure Analysis, 2010

The LP economiser lower header on a HRSG ruptured shortly after a diverter damper incident. Tetra was approached by the client to investigate the possible root causes for the rupture. The unit went into single element control at the time of the incident and the LCV cycled through fully open / fully closed positions to maintain the drum level after “shrink”. When the damper re-opened the LCV remained closed as the drum level increased (swell). The economizer temperature increased and there was an associated increase in pressure. The safety valve failed to operate as it was accidentally gagged, causing serious over pressurisation and a burst header.

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